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  • CN 62-1112/TF 
  • ISSN 1005-2518 
  • 创刊于1988年
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采选技术与矿山管理

球磨机细磨阶段钢段与钢球磨矿效果对比

  • 王旭东 ,
  • 肖庆飞 ,
  • 张谦 ,
  • 杨森 ,
  • 马帅
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  • 1.昆明理工大学国土资源工程学院,云南 昆明 650093
    2.矿物加工科学与技术国家重点实验室,北京 100070
王旭东(1995-),男,河南新乡人,硕士研究生,从事碎磨理论与工艺研究工作。852911345@qq.com

收稿日期: 2019-09-23

  修回日期: 2020-06-12

  网络出版日期: 2020-11-05

基金资助

国家自然科学基金面上项目“多级配球介质磨矿的能量匹配及机理研究”(51774157);矿冶过程自动控制技术国家(北京市)重点实验室开放基金项目“半自磨钢球配比及衬板形状优化模拟仿真技术研究”(201905);安徽省重点研究和开发计划面上攻关项目“复杂难处理铜(硫铁)矿清洁高效节能综合利用关键技术研究”(201904a07020044)

Comparison of Grinding Effect Between Steel Section and Steel Ball During Fine Grinding Stage of Ball Mill

  • Xudong WANG ,
  • Qingfei XIAO ,
  • Qian ZHANG ,
  • Sen YANG ,
  • Shuai MA
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  • 1.School of Land and Resources Engineering,Kunming University of Science and Technology,Kunming 650093,Yunnan,China
    2.State Key Laboratory of Mineral Processing Science and Technology,Beijing 100070

Received date: 2019-09-23

  Revised date: 2020-06-12

  Online published: 2020-11-05

摘要

针对大坪选厂细磨工段磨矿产品粒度均匀性差,磨矿细度-0.074 mm含量不达标,过粉碎含量偏高等问题,制定了磨矿介质制度优化方案,通过实验室磨矿试验得出细磨工段磨矿介质采用钢段效果更佳,其磨矿介质制度:Φ45×50∶Φ35×40∶Φ30×35∶Φ25×30=30∶20∶20∶30。试验结果表明:全面钢段方案与钢球方案及现厂方案相比,各项指标均得到一定的提高,过粗级别+0.10 mm产率分别减少了0.73个百分点和5.42个百分点,过粉碎级别-0.010 mm产率分别减少了2.51个百分点和0.77个百分点,磨矿细度-0.074 mm含量分别提高了1.75个百分点和5.33个百分点,中间易选级别0.100~0.038 mm产率分别提高了1.96个百分点和5.57个百分点,磨矿技术效率分别提高了3.54个百分点和8.14个百分点,磨机-0.074 mm利用系数分别提高了3.15%和10.24%。因此,根据试验前后各项指标对比,全面钢段更加适用于细磨工艺,能够有效改善“两端多、中间少”的现象,提高磨矿效率和合格产品质量占比。

本文引用格式

王旭东 , 肖庆飞 , 张谦 , 杨森 , 马帅 . 球磨机细磨阶段钢段与钢球磨矿效果对比[J]. 黄金科学技术, 2020 , 28(5) : 771 -777 . DOI: 10.11872/j.issn.1005-2518.2020.05.158

Abstract

The particle size of the grinding products in the fine grinding section of a domestic mineral processing plant is uneven,and there are more coarse-grained and over-fine-grained grades.At the same time,the content of the grinding fineness -0.074 mm does not meet the standard.According to the current mill grinding process,combined with the nature of the ore itself in the concentrator,the grinding quality is improved through the grinding process.This paper uses the international standard sieve for particle size screening of the ore sampled uniformly,combined with the spherical diameter semi-theoretical formula to formulate the grinding plan,compare the grinding results,evaluate and select the best grinding plan.Laboratory test results and data analysis show that the grinding media system is Φ45×50∶Φ35×40∶Φ30×35∶Φ25×30=30∶20∶20∶30. Compared with the steel ball plan and the current plant plan,the overall steel section plan has an over-coarse level of 0.10 mm and a yield reduction of 0.73 percentage points and 5.42 percentage points,respectively,and an over-pulverization level of 0.010 mm and a yield reduction of 2.51 percentage points and 0.77 percentage points,respectively.The grinding fineness -0.074 mm content has increased by 1.75 percentage points and 5.33 percentage points respectively.The intermediate easy-selection grade 0.100~0.038 mm yield has increased by 1.96 percentage points and 5.57 percentage points,respectively,and the grinding technology efficiency has been improved by 3.54 percentage points and 8.14 percentage points,mill q-200 increased by 3.15% and 10.24%.According to the comparison of various grinding indexes,it can be concluded that the grinding method of the steel section in the grinding process is mainly based on the grinding and peeling effect,supplemented by the impact effect,which can effectively reduce the content of coarse-grained and super-fine-grained grades,and improve the qualified grain.The level of content reduces the difficulty of flotation.The increase of the efficiency of grinding technology shows the improvement of the quality of grinding products,and the increase of the mill q-200 shows the improvement of the production capacity of the mill’s unit effective volume.The above conclusions indicate that the steel segment is more suitable for fine grinding process,it improve the quality of grinding products,the production capacity of the mill and the efficiency of the enterprise.

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